Calendar check middle of April 2018
I forgot to post in the last one when I did the pump I also installed the Radium FPR I had laying around from the Evo build that I never used. I modified the fuel rail to accept AN fittings so it is all very easy to take apart and looks good.
I sent my truck to a local fab guy and he built my fender exit exhaust. Made this version on April 30th, shows a little bit of the exhaust build and some two step just for fun.
https://www.youtube.com/watch?v=tyzkqS5hzkoAfter this, I made my way to the track.
With a new fuel pump, new converter and some drag radials I wanted to see what it'd do. I was expecting maybe a 11.6x type of pass.
And then it happened.
I staged and got on the 2step and it moved out. It was WAY faster to the 1/8th than I expected and the trans wasn't shifting as I was getting rev limiter between shifts. Somewhere just past the 1/8th I lost a bunch of power and it literally stopped accelerating at 114mph. I ran the last 500ft or so at that speed and chose to just stay in it to see what it would do.
Here's the result.
As for why I lost power: melted tip of spark plug #6 (it was loose) and timing was being retarded from false knock, chased down a pinched wire later
As for why it wasn't shifting right: bad TV cable to transmission
Here's some photos from track visit for fun. The Typhoon is my buddy Brian, he holds the stock engine, stock turbo record for a Typhoon at a 12.3 and is currently putting an LS swap in it.
The next steps at this point were to work out more bugs.
Fix the spark plug
Fix the knock sensor issue
Get boost to hold more steady (did some porting, changed wg springs, got manual controller installed)
My next post will be some runs after fixing a bunch of this stuff, getting a new chip from TT with some more drastic changes and has a video and some slips.