Just a little write-up on how I modified my manifold from a T2 flange to a T3 flange. I've posted some pics here, but figured I do a little write-up anyways. I'll be doing a longer one on repairing broken fasteners soon…
When I bought my manifold, it was T2 based and the threads where stripped. I had a T3 based turbo though. I looked into T2-T3 adapters, but with the lack of clearance I already had, adding a spacer wasn't an option. Plus adding a spacer/adapter means more failure points. But I got a deal on the manifold and didn't want to sell it and pay more money to get a shittier T3 manifold. Well, I measured and there was plenty of surface area for the manifold to have a T3 bolt pattern.
Before I did this, I searched and searched for this to find several people talk about it, but few said it would work, and I never found any pics of where someone actually did this or reported they did it and it held up. So I tried it and it works.
First, I needed to fill the old holes up. Since they were stripped, I first drilled them out and retaped them 3/8-16. This was easy as the stock holes were tiny anyways. Then I cleaned the threads and bolts up with brake parts cleaner applied some high strength lock-tite to the grade 5 bolts, and torqued them down into the manifold. After sitting for a day the lock-tite anchored the bolts into the manifold.
Then I just cut them off with a hacksaw. I used a file to surface the manifold to get the bolts back to flat and to take any warp out of the manifold. Now we're back to all metal.
Now I C-clamped a T3 flange I had to the manifold and used a 3/8 drill bit to mark my four holes (using a transfer punch would have been better, but this worked). Then drilled a pilot hole with a 1/8 bit, then drilled them tap size for 3/8-16, which is 5/16". I used a 1/20 HP drill press from Lowes so it was slow but it kept everything square, which is important.
I actually drilled into part of the bolt when retaping. That's why I lock-tite'd them into the manifold so they wouldn't try to spin out when the drill bit hit them. Worked. Then I tapped the manifold 3/8-16. The threads actually go into the manifold over 1" deep. This helps keep the fasteners from vibrating out. So does drilling and wiring them together though.
And that's pretty much it. I used grade 5 bolts and it wasn't hard to drill into surprisingly. Could have used a lower grade bolt and been fine probably though. Been running for almost 3 months so far and it's worked perfect. Cost me $1.20 for the bolts. Cheaper than a new manifold.
Pics..
Manifold as purchased for 118 shipped.
I retaped it for 3/8-16 and lock-tite'd new grade 5 bolts in it.
Then cut them off with a hacksaw
And surfaced it with a bastard file.
Then retaped the manifold to T3
Test fit
Works great. $120 T3 Cast FM manifold converted to T3.