FUCK!
We went out on monday night to make a ripper. I decided to hook up the manual boost controler and up the boost. My brother tuned in some more fuel, and we put a vise grip on the fuel return line to up the fuel pressure.
I did a nasty burn out, and a few launches. Up until then, it was running very strong, so we went out to I95 for some highway runs. As requested, I did a 3rd and 4th gear pull. This is when shit went down hill. I am not 100% on what fucked up, but something did. Smoke pourd out a million time worse than it already did, and I instantly lost power. Had to pull over and check it out. But it was dark and we couldn't see shit, so I had to baby it home, wich took forever at 20mph.
Today, we did a compression check, and it wasn't good. 150, 145, 90, 45. Had no choice but to tear it apart, hopping it was the headgasket. Wrong. 3 and 4 are toast. What realy sucks, it during the tear down, I find that this motor I bought was not just a head swap, but had new pistons.
I was so pissed, But I have a buddy with an a1 and ima snatch it up and do an OCZC rod/vitara dual cam.
uploading pics now