So...I went to the dyno today, with LeeD, well respected member of the local tuning community. It was going well basically until the car started making 275 or so hp, the car started going lean around 6600 rpm's.
So after 5 hours on the dyno, 2 walbro pumps, a brand new fuel filter, 2 regulators and I believe even trying massive duty cycle on the injectors, we gave up. Very frustrating, I'm tearing my hair out over this.
It can't be anything software wise, it has to be an electrical or mechanical issue.
Possibilities!?
-Injectors are bad? don't see how, precision 880's with 2000miles on them.
-Power supply weak to pump? didnt think stock wiring was an issue until closer to 500whp
-Regulator? Rail psi was at 45psi at one point and we watched it climb as boost came on, seems to be doing its job fine.
-Resistor box issues? 99% positive I have the wiring right.
-Clogged hard fuel lines? doubt it, but maybe?!
Setup is as follows:
Walboro 255
Precision 880's
Generic FPR
Innovative GT61s
Shitbird Manifold
Chingagate 38mm
Perrin MBC
Could you guys throw out some suggestions that I could try? because I have NO idea anymore.
Thanks Dave, Spiker, Marcus and everyone else for the help, I appreciate the amount of determination to get this shit box making some power. I'll get it, this is just a setback.