still nothing but problems with this pos
-ecu and vtec signal line switch every time consistently now.
-vtec would only work the first couple pulls until you let it set and cool off an hour, so I replaced my 1/4 OD hardline with a -6 stainless braided.
-Did a pull and power seemed off
-threw a timing light on to check base timing and see if the cams slipped and the car just shut off. MSD box is dead, and of course its a potted version that they can't fix.
-wired the stock ignitor to the MSD HVC coil and it runs again.
-did a pull around 13 psi, power was coming up faster than the 10 psi pull but leveled off just under 400 hp, don't know if something is still fucked or if its making power but spinning on the dyno
-at some point we threw a pressure gauge on the service port of the head, the vtec circuit is definitely getting pressure. So im pretty sure its working at this point.
I give up. Going to try a couple things tonight, see if it was spinning, see if it cooperates and makes some power. If not I'm trailering it home and going over everything again.
Some shitty vid of a random pull towards the end. don't remember
http://vid218.photobucket.com/albums/cc302/stenseltizm/CRX%202014%20Build/IMG_2408_zpscf277089.mp4